UNITED STATES
SECURITIES AND EXCHANGE COMMISSION
Washington, D.C. 20549
FORM 8-K
CURRENT REPORT
Pursuant to Section 13 or 15(d) of the
Securities Exchange Act of 1934
Date of Report (Date of earliest event reported): March 24, 2006
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Exact Name of Registrant as Specified in |
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Charter; State of Incorporation; |
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IRS Employer |
Commission File Number |
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Address and Telephone Number |
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Identification Number |
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1-8962
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Pinnacle West Capital Corporation
(an Arizona corporation)
400 North Fifth Street, P.O. Box 53999
Phoenix, AZ 85072-3999
(602) 250-1000
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86-0512431 |
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1-4473
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Arizona Public Service Company
(an Arizona corporation)
400 North Fifth Street, P.O. Box 53999
Phoenix, AZ 85072-3999
(602) 250-1000
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86-0011170 |
Check the appropriate box below if the Form 8-K filing is intended to simultaneously satisfy
the filing obligation of the registrant under any of the following provisions:
o Written communications pursuant to Rule 425 under the Securities Act (17CFR 230.425)
o Soliciting material pursuant to Rule 14a-12 under the Exchange Act (17 CFR 240.14a-12)
o Pre-commencement communications pursuant to Rule 14d-2(b) under the Exchange Act (17 CFR
240.14d-2(b))
o Pre-commencement communications pursuant to Rule 13e-4(c) under the Exchange Act (17 CFR
240.13e-4(c))
This combined Form 8-K is separately filed by Pinnacle West Capital Corporation and Arizona
Public Service Company. Each registrant is filing on its own behalf all of the information
contained in this Form 8-K that relates to such registrant and, where required, its subsidiaries.
Except as stated in the preceding sentence, neither registrant is filing any information that does
not relate to such registrant, and therefore makes no representation as to any such information.
Item 8.01. Other Events
Palo Verde Nuclear Generating Station
As previously reported, Arizona Public Service Company (APS) has been operating Unit 1 of
the Palo Verde Nuclear Generating Station (Palo Verde) at reduced power levels since December 25,
2005 due to vibration levels in one of the Units shutdown cooling lines. A planned outage began
March 18, 2006, during which inspections and tests were
performed in preparation for a then expected
five-week outage in the June timeframe (June Outage) during which necessary modifications would be made to the
Unit to remedy the situation. See Palo Verde Nuclear Generating Station in Item 8.01 of the
APS/Pinnacle West Capital Corporation (Pinnacle West) Current Report on Form 8-K filed on March
7, 2006.
APS has determined that
certain work can be advanced so as to provide
greater assurance that the Unit will be operating during the peak
summer months and somewhat accelerate the expected timeframe for returning the Unit to full
power. As a result of tests performed during
the last week, APS has determined that vibration limits could be
exceeded under a limited number of operating scenarios. Consequently,
rather than pursue operating modifications to bring the Unit back
into service, it will undergo pre-work and additional engineering
tests supplemental to the previously planned June Outage.
APS previously
estimated that the June Outage and Unit 1s reduced power levels since January 1, 2006
would result in incremental replacement power costs of approximately $58
million after income taxes and that approximately $50 million of such amount
would be deferred for future rate recovery under APS regulatory power supply adjustor
(PSA). APS now estimates that after-tax incremental power costs and PSA deferrals will be approximately $46
million and $41 million, respectively, reflecting Unit 1s potential earlier return to full power
and exceptionally strong performance from APS other generation units.
Forward-Looking Statements
This document contains forward-looking statements based on current expectations, and neither
Pinnacle West nor APS assumes any obligation to update these statements or make any further
statements on any of these issues, except as required by applicable law. These forward-looking
statements include statements regarding (i) the timing and duration of the planned Unit 1 outage;
(ii) the incremental purchased power and operations and maintenance costs associated with Unit 1s
reduced power level and outage; and (iii) the amount of PSA deferrals resulting from Unit 1s
current situation. Because actual results may differ materially from expectations, we caution
readers not to place undue reliance on these statements. A number of factors could cause future
results to differ materially from historical results, or from results or outcomes currently
expected or sought by Pinnacle West or APS. These factors include, but are not limited to, (a)
increased prices for purchased power; (b) unanticipated technical or operational issues associated
with Unit 1s current situation; (c) unanticipated increased costs associated with Unit 1s current
situation; and (d) the possibility that the Arizona Corporation
Commission may not permit APS to fully recover the PSA
deferrals resulting from Unit 1s current situation.